GreekGod
09-11-2007, 12:08 PM
click on Link to view photos:
http://www.network54.com/Forum/74182/thread/1189515768/Drag+Week+2007%2C+Day+1+at+Cor dova
<TR><TD style="PADDING-TOP: 4px" valign="top" colspan="2">Drag Week 2007, Day 1 at Cordova</TD></TR><TR><TD valign="bottom" colspan="3">
<HR></TD></TR><TR><TD colspan="3"><!-- google_ad_section_start -->Day 1 of Drag Week 2007 is in the books, and for me so far it has been a strenuous exercise. Please allow me to backtrack to yesterday, test and tune day, to recount all the grisly details.
You may recall from my previous post that we lost the front bearing on the blower about fifty miles from Cordova on Saturday night. Joel and I had removed the belt and run the rest of the way to the hotel unsupercharged, and I had been pretty happy with how the car performed without the blower hooked up. Sunday morning we were up bright and early, ready to go to the test and tune, swap in the spare blower, and make some passes.
We drove the 10 miles or so to the track from our hotel, and arrived about 8:00. After registration for the event, I got busy tearing the damaged supercharger out of the car in order to replace it. But when I pulled the air cleaner assembly and hat off the carb, I got a very nasty surprise:
That little hunk of aluminum in the booster venturi is NOT supposed to be there. It was obviously a piece of the supercharger’s impeller. Next I looked straight down the throat of the carb, and was shocked to see a whole bunch more of the stuff sitting on top of the secondary throttle plates. Lucky I kept my foot out of it for the last 50 miles to Cordova! Here’s a photo of the shrapnel I poured out of the carb when I removed it from the engine:
It was indisputable now that the engine had ingested a large volume of shrapel. Yet, it appeared to be running just fine. I decided that I’d better do a thorough check of the motor, so I pulled all the plugs and the valve covers, and took my time examining the inside of the intake manifold. The intake was clean, and the valvetrain looked fine, with all the last adjustments just as I’d previously set them. The only indication of any problem was with the #4 plug, whose gap had closed up from .035 to about .020.
Back at the BP station on Saturday night, after pulling the blower belt I had removed the top of the supercharger’s inlet box to take a look at the impeller blades. Everything had looked fine. When I pulled the blower now, I saw the problem. The Vortech V7-YSi blower has two sets of impeller blades, in a double row configuration. With the blower laying on the ground, it was clear that while the outside row was undamaged, the inside row was chopped up pretty good. The impeller blades on the outside row were the only ones I could see by looking into the top of the inlet box when the blower was on the car.
Feeling like I’d dodged a bullet, I replaced the blower with my undamaged older unit, and reassembled the car. When I started it up, everything seemed find, and the new blower was very quiet as compared with the previous one. By this time it was around noon, and I finally was able to get into the tech line. The deadline for getting through tech to qualify for Drag Week was 2:00 PM on Sunday, so I'd made it with a couple of hours to spare.
Preparing for tech, I had a temporary NHRA drivers license since I hadn't received my permanent one in the mail yet. The chute was on the car, I'd changed the window net mounting location and also the submarine strap mounting location per instructions from the tech guy at Rock Falls two weeks ago. I'd never gone through tech with the car in this configuration before, and with just a temporary NHRA license I was afraid that the tech people might flag me for something that I'd done wrong on the chute or whatever. As it turned out, when the tech guy showed up he hardly looked at anything, not even my NHRA license! He just took a quick look at the car, checked my helmet and belt dates, and wrote 8.50 on the tech card. That number was important, because Hot Rod won't accept any times faster than the lowest ET shown on the tech card from Cordova.
From tech we went to the Hot Rod check in, where they did their own "street legal" tech. Here they were going to check for headlights, brake lights, turn signals, horn, and wipers. While waiting in line I snapped this photo of a nice 63 Galaxie and my car together:
Unfortunately the Gal didn't have an FE, but it did have a 514" 385 series engine in it, and from what the owner said it ran pretty good, mid 11s I think.
After waiting in line for an hour, I finally got through the Hot Rod tech. I got a chance to talk a little with David Freiburger while he was checking over my car. Joel knows David as well, from his involvement with the F.A.S.T. class, so it was fun for all of us to get caught up.
By now it was after 1:00, and the test and tune was underway, so back in the pits I got ready to make a pass with the car. This was going to be the acid test; did I really do any damage with the blower explosion? How would the car run? What affect would the change to the 3.50 gears have? How would my A/F be after jetting the carb down?
Only one way to find out, so I went up for a pass. The line wasn't too long, and before I pulled into the burnout box I made sure that my LM-1 was recording so that I got good A/F data. Immediately upon launching the car, I knew that going to the 3.50 gears had been the right choice. The car still spun on the line, but much less than it ever had before, and more importantly it stayed straight. As it turned out my 60' time for this run was about 1.54. Down the track I ran it to the 6200 RPM shift point, did my 1-2 shift and held my breath. Previously the car had tended to break the tires loose on this shift; not anymore. The car shifted clean and stayed straight, and I knew I was in the middle of a good pass. Then, at about 1000 feet - the car just quit pulling. It felt like I'd run out of fuel or something! I backed out of the throttle and coasted past the finish line. On the return road the car acted normally, and the slip said 10.14 @ 110 MPH. I pulled into the pits wondering what could have gone wrong. When I popped the hood, I was relieved to see that the blower duct tubing had come loose. Apparently I had forgotten to tighten one of the band clamps on the rubber coupling hose going into the hat. No wonder the car quit pulling.
I tightened up the clamp and let the car cool. I downloaded the log from my LM-1, but the data didn't make any sense. It didn't even appear that the pass was recorded properly, so I didn't get any A/F information. That was disappointing; I had really wanted to monitor that. I cleared the LM-1 memory, figuring I would just have to try again.
see part II...</TD></TR>
http://www.network54.com/Forum/74182/thread/1189515768/Drag+Week+2007%2C+Day+1+at+Cor dova
<TR><TD style="PADDING-TOP: 4px" valign="top" colspan="2">Drag Week 2007, Day 1 at Cordova</TD></TR><TR><TD valign="bottom" colspan="3">
<HR></TD></TR><TR><TD colspan="3"><!-- google_ad_section_start -->Day 1 of Drag Week 2007 is in the books, and for me so far it has been a strenuous exercise. Please allow me to backtrack to yesterday, test and tune day, to recount all the grisly details.
You may recall from my previous post that we lost the front bearing on the blower about fifty miles from Cordova on Saturday night. Joel and I had removed the belt and run the rest of the way to the hotel unsupercharged, and I had been pretty happy with how the car performed without the blower hooked up. Sunday morning we were up bright and early, ready to go to the test and tune, swap in the spare blower, and make some passes.
We drove the 10 miles or so to the track from our hotel, and arrived about 8:00. After registration for the event, I got busy tearing the damaged supercharger out of the car in order to replace it. But when I pulled the air cleaner assembly and hat off the carb, I got a very nasty surprise:
That little hunk of aluminum in the booster venturi is NOT supposed to be there. It was obviously a piece of the supercharger’s impeller. Next I looked straight down the throat of the carb, and was shocked to see a whole bunch more of the stuff sitting on top of the secondary throttle plates. Lucky I kept my foot out of it for the last 50 miles to Cordova! Here’s a photo of the shrapnel I poured out of the carb when I removed it from the engine:
It was indisputable now that the engine had ingested a large volume of shrapel. Yet, it appeared to be running just fine. I decided that I’d better do a thorough check of the motor, so I pulled all the plugs and the valve covers, and took my time examining the inside of the intake manifold. The intake was clean, and the valvetrain looked fine, with all the last adjustments just as I’d previously set them. The only indication of any problem was with the #4 plug, whose gap had closed up from .035 to about .020.
Back at the BP station on Saturday night, after pulling the blower belt I had removed the top of the supercharger’s inlet box to take a look at the impeller blades. Everything had looked fine. When I pulled the blower now, I saw the problem. The Vortech V7-YSi blower has two sets of impeller blades, in a double row configuration. With the blower laying on the ground, it was clear that while the outside row was undamaged, the inside row was chopped up pretty good. The impeller blades on the outside row were the only ones I could see by looking into the top of the inlet box when the blower was on the car.
Feeling like I’d dodged a bullet, I replaced the blower with my undamaged older unit, and reassembled the car. When I started it up, everything seemed find, and the new blower was very quiet as compared with the previous one. By this time it was around noon, and I finally was able to get into the tech line. The deadline for getting through tech to qualify for Drag Week was 2:00 PM on Sunday, so I'd made it with a couple of hours to spare.
Preparing for tech, I had a temporary NHRA drivers license since I hadn't received my permanent one in the mail yet. The chute was on the car, I'd changed the window net mounting location and also the submarine strap mounting location per instructions from the tech guy at Rock Falls two weeks ago. I'd never gone through tech with the car in this configuration before, and with just a temporary NHRA license I was afraid that the tech people might flag me for something that I'd done wrong on the chute or whatever. As it turned out, when the tech guy showed up he hardly looked at anything, not even my NHRA license! He just took a quick look at the car, checked my helmet and belt dates, and wrote 8.50 on the tech card. That number was important, because Hot Rod won't accept any times faster than the lowest ET shown on the tech card from Cordova.
From tech we went to the Hot Rod check in, where they did their own "street legal" tech. Here they were going to check for headlights, brake lights, turn signals, horn, and wipers. While waiting in line I snapped this photo of a nice 63 Galaxie and my car together:
Unfortunately the Gal didn't have an FE, but it did have a 514" 385 series engine in it, and from what the owner said it ran pretty good, mid 11s I think.
After waiting in line for an hour, I finally got through the Hot Rod tech. I got a chance to talk a little with David Freiburger while he was checking over my car. Joel knows David as well, from his involvement with the F.A.S.T. class, so it was fun for all of us to get caught up.
By now it was after 1:00, and the test and tune was underway, so back in the pits I got ready to make a pass with the car. This was going to be the acid test; did I really do any damage with the blower explosion? How would the car run? What affect would the change to the 3.50 gears have? How would my A/F be after jetting the carb down?
Only one way to find out, so I went up for a pass. The line wasn't too long, and before I pulled into the burnout box I made sure that my LM-1 was recording so that I got good A/F data. Immediately upon launching the car, I knew that going to the 3.50 gears had been the right choice. The car still spun on the line, but much less than it ever had before, and more importantly it stayed straight. As it turned out my 60' time for this run was about 1.54. Down the track I ran it to the 6200 RPM shift point, did my 1-2 shift and held my breath. Previously the car had tended to break the tires loose on this shift; not anymore. The car shifted clean and stayed straight, and I knew I was in the middle of a good pass. Then, at about 1000 feet - the car just quit pulling. It felt like I'd run out of fuel or something! I backed out of the throttle and coasted past the finish line. On the return road the car acted normally, and the slip said 10.14 @ 110 MPH. I pulled into the pits wondering what could have gone wrong. When I popped the hood, I was relieved to see that the blower duct tubing had come loose. Apparently I had forgotten to tighten one of the band clamps on the rubber coupling hose going into the hat. No wonder the car quit pulling.
I tightened up the clamp and let the car cool. I downloaded the log from my LM-1, but the data didn't make any sense. It didn't even appear that the pass was recorded properly, so I didn't get any A/F information. That was disappointing; I had really wanted to monitor that. I cleared the LM-1 memory, figuring I would just have to try again.
see part II...</TD></TR>